Posts Tagged ‘problem solving’
Busted Brackets
Upon closer inspection of the mounting system on the ATV plow blade, I discovered significant mechanical failures. I completely missed it when I became overly focused on not being able to slide the pin back to change the blade angle. The two brackets that hold a pulley had fractured and then bent.
Oops. No wonder things weren’t working as well as they used to.
I took everything apart, lubricated the pin to make sure it moved freely, and then retrieved the U-bolt that had previously served as the winch cable attachment point. Replacement brackets were going to cost more money than I wanted to spend, so I’m reverting to the old way, with one added trick I’ve learned.
Those brackets that broke held a pulley that increases the mechanical advantage for lifting the blade. I found that I already have a pulley I can use that won’t require a bracket to get the lift I’m seeking. That problem is solved; however, the pin is still getting hung up somehow, so I can’t change the angle of the blade yet.
A little more tinkering needs to happen today. I ran out of daylight by the time I got around to testing the reassembled hardware yesterday. If I can figure out what’s keeping that pin from sliding easily and resolve the issue, I’ll be back in business for plowing snow.
Just in case we get another dose of snowflakes piling up more than a trace amount.
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Custom Solution
We were moving our gas grill off the deck when one of the doors fell to the ground. Cyndie found a bolt with a nut on it lying there, but I couldn’t figure out what had broken or how it had been attached. As far as I could tell, the bolt was just functioning as a post that the door pivoted on. First impression was that a new bolt would solve the problem, but I knew it was more complicated than that.
There wasn’t a way to screw a replacement bolt back on, so the trick would be to mount the bolt in a way that would leave just the threaded portion exposed to mate with the hole in the bottom corner of the door.
Based on the space I was working with, it would likely require a very thin nut. One possibility would be to grind down a standard-width nut to something much skinnier, but I had another idea.
I found a washer with a center hole one size smaller than the replacement 1/4-20 bolt I was going to use. I planned to try tapping threads into that washer. My first challenge was how to hold that little washer in order to cut threads into it.
After a couple of failed attempts to clamp it directly into a bench vise, I pinched the edge of the washer with a vise-grip pliers and then clamped the pliers into the bench vise. The little washer was just thick enough to accept a fraction of threads, and that proved to be enough to spin it on the bolt.
I don’t know if you were able to follow all that, but in the accompanying photo, the little washer I tapped is directly between the bottom of the door and the brown portion of the grill frame. Somewhat to my surprise, it worked to hold the bolt that is coming from below to protrude up into the door.
That’s all I needed. Color me chuffed. I had paused mowing to help move things back onto the deck and then ran into this nuisance of a task. My goal was to find a quick fix and get back to mowing. Given all the steps I ended up taking, it was quick enough and successful enough, and gave me a boost of satisfaction that my ingenuity produced a custom solution that worked on the first try.
The experience acquired from a career in manufacturing continues to pay dividends in my retirement. I bought us a little more time with that old grill, but its days are numbered. It is admittedly well beyond its “Best If Used By” date.
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Months Later
You could call it “John Standard Time.” Sometimes it takes a while for me to execute. Here is a pretty good example…
The story has a background that goes back years. Many years ago, in fact. The old day job in manufacturing had a small bandsaw purchased from Harbor Freight for cutting metal. One day, the switch burned out, and the owner opted to simply replace the saw with a new version of the same model.
I’m not sure what got into me, but I told him I could take the old one off his hands to save him from figuring out how to dispose of it. I found a replacement switch and had myself a very inexpensive saw for my shop. In the last decade, I’ve used it to cut metal only once or twice. A couple of times, I used that metal-cutting blade to cut wood. It was slow, but it worked.
That inspired me to look into buying a bandsaw blade intended for cutting wood, even though that wasn’t what this saw was designed to do. The speed wasn’t as fast as it should be, but since I had some success misusing the metal-cutting blade, I figured it was worth trying to undercut the specs on a wood-cutting blade without a major loss if it didn’t work out.
Not knowing anything about what I was doing, I called to speak to a blade expert at a company I found online. He was kind enough to educate me to the point of being able to pick a blade for my experiment, even though he knew I didn’t have the correct bandsaw for the job.
By Christmastime last year, I was pressured to come up with a wish list of ideas for gifts I’d appreciate, so I put the blades on my list. Surprise! I got a box with two perfect wood-cutting bandsaw blades.
It took me another five months or so to get around to installing one of the new blades on the saw. That exercise was not a pretty sight. I had no clue what I was doing and fumbled my way through several failed attempts, and gained multiple irritating cuts on my fingers.
Then, I ran into a problem when I tried to move the belt on the pulleys to the fastest speed. The two pulleys in the diagram on the saw appear to be installed in opposite orientations, but the actual pulleys on the saw were installed identically to each other.
I let another month pass until I had a chance to ask the advice of friends with mechanical knowledge. One of them knew the exact bandsaw. They agreed that one of the pulleys was on wrong and told me it was easy to fix.
Two months after that, I got around to trying to find the set screw that holds the pulleys on the shaft of the motor. It took some tenacious hunting, but I found it, and after many tries in low light, found the Allen wrench that fit.
A few days ago, I made my first attempt to cut wood. It worked like a warm knife through butter. Merry Christmas!
Look out world, I’ve got a whole new weapon in my low-tech woodworking hobby.
Why, in a few months or twelve, I might finish making another snazzy woodgrained something-or-other.
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Not Panicking
Just because my pet maple tree that we transplanted to the middle of the labyrinth hasn’t sprouted leaves yet, while almost every other tree around has, we’ve chosen not to panic. New buds are visible, but they just haven’t made as much progress as we expect at this point. There are a small number of other trees of a variety of species that are similarly delayed compared to the majority of broadleaved trees and bushes around here, so there is that. It’s not alone.
Since we have been enduring a long span of hot, dry, sunny days, our cool-headed response to the situation was to put a watering bag around the trunk to keep the little guy well-hydrated. We are hoping to see visible progress of advancing leaf buds soon.
I had another opportunity to not panic yesterday afternoon while mowing. As my confidence and control on the zero-turn riding mower have improved, I find myself pushing beyond some of my previous boundaries. I’ve started mowing a half-swath beside some of our pathways with the deck at the highest setting to control the walkway narrowing from tall grass on the sides bending over into the lane.
Cutting it back with the riding mower is a great improvement over my previous effort of walking along and swinging the hedge trimmer blades across the too-tall grasses after the fact. That is laborious, back-aching work.
While making a first pass along the edge of our path around the back pasture and hay field, the front wheels suddenly jumped, and the mower deck bottomed out on a tall mound. The mower was pointed down into a bunch of scrub brush trees along the drainage swale. With the deck stuck on the mound, the drive wheels had no grip on the ground. I couldn’t move forward or reverse.
I do believe my years of experience were revealed in a complete lack of cursing and tantruming. I simply walked all the way back to the shop and got the ATV and a come-along. After a couple of futile tries, I realized I needed Cyndie’s help. I pulled out my phone to call her and found she had texted me.
“We’re walking off leash & see you on ATV- need help?”
Since she has never operated the zero-turn, I offered her the ATV, and I spun the wheels on the mower. Nope. No progress, but I had a hunch.
I asked her to try the mower, and I got on the ATV. The throttle just needed to be goosed with a little more oomph, and we pulled it right off that mound.
When success comes without having put myself through the angst of getting overly upset at the outset, the reward of solving the dilemma is that much sweeter.
It pays not to panic.
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Crown Complete
You know what else feels lovely? Having a long-awaited project completed. We’ve known for a few years that the crown on top of our chimney was compromised, the cement cracked and allowing water penetration when it rains and snows. The kind of issue that was invisible to us on the ground and could have lingered unknown for a long time before it emerged as very costly structural damage to the whole chimney.
During a regular chimney cleaning appointment, we were informed the crown was aging poorly. That chimney sweep told us he fabricates metal crowns that can be placed directly over the existing cement.
Sounded good to me in my total niaveté. Sign me up! Of course, this happened in the fall, and the guy said he was way behind on making these custom chimney caps, so he could not predict when he would get to us.
After about a year of waiting with the nagging concern that water was seeping in with each bout of precipitation, I called to see what his schedule looked like.
He ghosted me. ‘Nuff said. We asked for an assessment from a more reputable company this fall, and now the problem is solved.
It is quickly obvious when you have landed a contractor who knows what he is doing. One who efficiently solves complexities and quickly achieves good results.
I never noticed that the old crown didn’t look all that impressive until the unveiling of the new one. With fabrication complete, they spent a few hours sealing the new cement and then continued all the way down to the bottom, covering the stones and masonry with a fresh coat of sealant for protection against the elements.
I love that we have one less concern in our ongoing quest to protect our place from water damage.
Looking at the weather forecast for the next few days, I happily say, “Let it rain and snow!”
We’ll build a nice warm fire and watch the precipitation with one less worry.
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Didn’t Happen
We somehow got missed by the passing snowstorm overnight Monday. Looking at the radar map from the comfort of our bed had me suspecting we were getting a fair dose of flakes. I figured there would be some shoveling to do at the very least when we headed out to feed the horses.
Much to my surprise, the number of flakes on our front steps was so paltry, there was open space between each one. It was like a cloud had sneezed and that’s all there was to show for it.
That’s okay. With no real foundation amount of snow this year, an occasional few inches ends up being more of a nuisance than anything fun. Plus, since snow didn’t happen, it gave me more time to prepare the ATV for eventual plowing. In my post yesterday, I mentioned that the electric lawn tractor was blocking the ATV and wouldn’t move due to some fault revealed by an error code. I couldn’t even get the drive wheels to release by the manual override that would allow me to simply muscle it out of the way.
Well, a second try proved to be the charm. I’m not aware of having done anything different, but when I tried again to pull the two levers that stretch a spring disengaging each drive wheel yesterday, it worked on my first try. I pushed the lawn tractor out of the way and drove the ATV out.
That success allowed me to hook up the trailer and finish hauling away all the branches I’ve trimmed off in the last month. The north loop pine tree project is officially completed for the season.
And, the ATV is now front and center in the shop garage.
You can see by the photo I took yesterday how much snow cover we have after receiving virtually none from the storm that passed just to our southeast. Weather forecasters suggest a plowable amount of snow is on the way for Friday.
I’ll believe it when I see it.
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No Worse
Things being “no worse” is not a ringing endorsement of happiness but I’m claiming it as a victory. There was no sign of water on the floor in the laundry room one day after Cyndie had cleaned it all up. Instead of blindly calling any plumber to help us diagnose a potential problem with the water softener, I figured I should at least try to learn enough about it to discuss its functions.
In searching online for a manual, I learned of a company in Red Wing that services our model. Without needing to see it in person, a plumber talked me through testing the “regen” operations over the phone. At each step, he could tell me where to look for the possibility of leaking water.
The good news is that by his analysis, the softener was unlikely to be the source of the leak. The bad news is we are now even more confused about where the water had come from to soak all our throw rugs. The plumber offered his thoughts about other possible causes, but nothing definitive came of it. For now, we are hovering in an observation mode and not returning any rugs to the floor.

Asher kept busy by familiarizing himself with a new pull-apart toy Elysa gave him for Christmas. I think he’s getting the hang of it.
My project for the ethernet cabling to the Wi-Fi repeater faired much better than being labeled, “no worse.” I reviewed the wiring in the last connector I crimped, using a magnifying glass, and deemed it visibly faultless. That led me to dig deeper into the software initialization of the hardware.
In a phone conversation with Julian, we were making our way through the connections and I climbed up to look one more time at the original router and associated hardware on top of the desk shelf in the den. The answer appeared right before my eyes. I had failed to plug in an RJ45 connector that I had disconnected when testing the attic cabling.
2024 is already looking better for us on day 3.
After succeeding with the repeater, my next step shifted to getting the camera mounted and connected to AC power down at the barn. I was thrilled to find the horses curious but not the least bit disturbed by my showing up with unfamiliar tools, making potentially scary sounds, and focusing on my task when they were expecting me to be serving feed for them.
I couldn’t finish last night, but completing the camera installation should be in reach today. Although, I am beyond committing myself to actually reaching such a goal.
At this point, I’m leaning toward seeking to make things ‘no worse’ for two days in a row. I’m on a roll!
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